Sunday, August 26, 2012

Noise Test and Engineering Checks

This weekend I took the car back up to see the engineer in Orange. It spent a day in the workshop on the hoist for all the engineering checks, and I now have a list of 7 things I need to fix or change....nothing to onerous.

Todays tests involved rerunning the noise tests I had previously failed. With a revised exhaust, new airbox and some more insulation, the car passed the tests, coming in under the 77db drive by tests and the 90db stationary test.

Getting very close now to a finished engineering report and hopefully a VIN and plates!

Saturday, August 11, 2012

Heat shield

After fitting the new air intake, I noticed how quickly the intake piping was getting hot, caused by the proximity of the headers. Given that I don't want preheated air going into the engine, and I have silicon joiners on the air intake, I decided to fit some heat shielding. 

I fabricated up some support brackets to sit between the headers and the intake to hold the shield, then shaped a piece of heat shield to fit it in the gap. Its tight at the front, but has a good air gap for most of the length of the intake and it protects the joiners.

Today has been spent fitting a new quieter exhaust and heat shields....photos to follow. The car is almost ready for its next and hopefully final engineering checks prior to rego!



Wednesday, July 25, 2012

Air Intake

One of the main reasons I failed the first noise test was induction noise. I had a pod filter directly connected to the throttle body, with no air box or resonators. When you nudged the throttle, you could hear it take a breath and gulp air in. On sharp throttle inputs it made very impolite noises, and on wide open throttle it whistled like it had a turbo. To fix all of this I have plumbed in a factory airbox and resonator up in the nose cone, and the routed air piping back to the throttle body. This is the 2.75" aluminum and blue silicone joiners you can see in the photo.  Because of the height of the engine and the intakes on the passenger side, I have had to route this plumbing down the less ideal drivers side, directly above the exhaust headers. To deal with the heat, I have fabricated brackets to keep the plumbing off the headers, and also some additional brackets between the block and the chassis. These are to hold up a heat shield that will keep the headers and the plumbing separate.

The net result is that there is now zero induction noise at idle, and no change in noise for any throttle position....problem solved!

p.s. Also noticed we passed 10,000 page views this week! Thanks to everyone who has followed this build and checked back in on the progress.


Wednesday, June 27, 2012

Engineering - Part 2 (Emissions)

Today was emissions testing. I had to pass the RTA's IM240 test certification which is the equivalent of Euro 2 emissions testing.  Given the engine has no mods and uses the factory ECU, tune and intakes and I have a Euro 3 spec CAT, it should be pretty easy to pass. And it was! It passed with virtually no emissions, with all the key numbers being so far below the max. The test did show up some interesting NOX levels on hard acceleration and a bit of fuel dumping on sudden overrun. Something to work on with the tuner, but its another major milestone passed!

Sunday, June 24, 2012

Engineering - Part 1


Last Sunday was the first day of engineering tests. I needed to do some last minute modifications to the exhaust heat shield on Saturday to stop a resonant vibration. Steve "the welder" made short work of this problem. The engineering tests took place some 300km from home, so it was up early on Sunday to load up and head out. It rained all day Saturday, so I was not able to load the car the day before. This meant loading up at 3:30am in the dark and wet. The car got even more wet on the 4 hour trip but I got there on time. 

Upon arriving at the test location, the first challenge was to cross a muddy red clay field to get to the track. Luckily I was towing with a 4wd, but churning across the paddock got the Birkin pretty dirty as it was sitting directly in the path of the flying mud. After unloading the tests begun. There was a whole bunch of other cars being tested including one other Clubman, a scratch build running a Zetec. It was 6 degrees celsius where we were testing, so it was a pretty long day standing around in the cold waiting for my test. 

Once it was my turn to go I already had the car warmed up and the V-box Racelogic system was installed to do the measurements. The engineer was doing a range of tests including general driving, braking, lane change/stability and noise (stationary and moving). It was a pretty proud moment to see my little car drive down to the end of the test track then come flying back up the strip in anger and full voice. Here's a clip of it making its second pass in to the braking test, which requires 15 consecutive stops from certain speeds, where each time it must stop inside a specific distance under a certain pedal load.

It passed the braking tests easily which is fantastic given the brakes were brand new and haven't even been properly bedded in. It passed the lane change and stability tests, although it whacked a cone on the first run. Due to Greg Fraser's (Redback Motorpsorts) work, the tyres didn't even chirp as it was hurled through the lane changes at increasing speed. Alas it failed the noise test, but more so on the induction air box noise rather than the exhaust. It is making some fairly high frequency noise on intake so this is not surprising. Not to worry as I needed to go back for other checks anyway. All in all a long day with another 4 hour drive home in the rain and dark. I now have a very dirty little car!!!!

Next test is this Wednesday, which is IM240 emissions. Stay tuned!


Tuesday, June 12, 2012

Shakedown - Part 2

In Shakedown - Part 1, I had 3 things to fix after my first real drive.
  • Broken headlight globe
  • Stuck closed thermostat
  • Broken exhaust mount
The headlight was easy to fix. The globe broke due to the vibration in the lens. I removed the whole light, replaced the globe, and then tightened the spring clips in the lens holder. Fixed.
The thermostat was harder. It involved a complete drain of the cooling system, removal of all the hose clamps, nose cone, fan belt and idler pulley. 3 bolts took 3 hours to remove! I tested the new thermostat before fitting, and the same 3 bolts took another 90 minutes to reinstall and torque. It was then just a case of replacing the other parts I had removed. Refilling with coolant took two nights of bleeding the air out of the system until the coolant level stabilised.

I used some fencing wire to hold the muffler on so I could test drive it and check the thermostat. Good news, the temperature stabilised at around 95 and held and the lower radiator pipe was also warm after 15km.

The problem with the muffler was that it had been hard mounted to the chassis (not by me). This meant that there was no isolation from vibration, so something had to give. The chassis mount was welded direct to the muffler body, and this broke after 20km, and it also bent the mount pretty badly. To fix this I got a rubber mount, and Steve the welder fabricated up an S bracket. We bolted the rubber mount onto a thicker chassis mount, and then welded the S bracket to the muffler body. We also took the S bracket a lot further under the muffler body and shaped it around the muffler allowing it to be welded on 3 sides (tripling the amount of welded joint). I then cut an adjuster slot into the chassis mount and bolted it up to the car. The chassis mount acts as a cantilever, and the whole thing is a lot more secure than before, but it also now has a vibration damper. I look forward to another test drive and hopefully it will last a bit longer than 20km.



Sunday, June 3, 2012

Workshop Fitout

On top of the lessons learnt, I thought I would share the additional tools I have used or added to the workshop during the build. This will give new builders an idea of what is needed beyond spanners.

  • Engine crane - rated to 750kg with adjustable boom and castors. I used this to lift the car a lot as well when fitting the engine
  • Engine stand - for dressing the engine before it goes in the car
  • Trolley jack - spend as much as you can and get one with as much lift as possible
  • Chassis stands - height adjustable with fine screw adjustment.
  • Digital vernier calipers
  • Hex head sockets - better than Allen keys!
  • Torque wrenches - I have two, one with a smaller range and one with a much larger range for big jobs like flywheel bolts
  • Sharp set of side cutters
  • T-bar - with connectors for sockets or hex bits
  • Stepper drill bits - for carefully enlarging holes out to as big as 22mm
  • Quality soldering iron
  • Electrical wiring crimper (good quality)
  • Auto electrical specific multi-meter
  • 1mm metal cutting wheel for the grinder
  • Fine tip paint pen in a bright colour - for marking position or marking torqued nuts/bolts
  • Good files for rough shaping of aluminum or steel brackets
  • Dremel - used for everything! From cutting, finishing, sanding, grinding
  • Rivnut gun - an expensive luxury best shared with a friend!
On top of this I had the usual set of ring and open ended spanners, sockets and screw drivers. I added quite a few larger spanners and sockets for jobs like fixing the upright ball joints, or tightening hub nuts. Most of these can be added as needed, but I can't emphasise enough the importance of using the right tool for the job. A vice and bench grinder is also handy.


One of the things I thought I would use a lot more was my compressor. I already had a rattle gun and I also got an air powered socket wrench. I guess the capacity and duty cycle was a little low on my compressor as it was more of a pain to use than being of any great benefit. I ended up using a cordless driver with socket attachments a lot more than anything else.



Lessons learnt

I have been meaning for a while to create a list of things I have learnt along the way. The aim of this is to warn new builders of some of the traps I fell into, and show some of the tricks I learnt along the way. Some of this is common sense, some of it is the result of hours of rework. I was never able to find a list like this, although many of these answers are scattered across countless forums and build diaries on the Internet. 

  • Check every package and delivery the moment you receive it to make sure its all there, and its what you ordered.
  • Understand the order of all tasks and the priorities they have to be done in.
  • Never put a task off until later because it's to hard. Do it in the right order.
  • Avoid putting all the body panels on as soon as you get it "just to see what it looks like"......huge waste of time (I never did this ;)
  • Where possible test fit each part for alignment before fixing or tightening.
  • Use copper grease on all splines
  • Use Loctite on all bolts
  • Check and replace spigot bearing ($5 bearing at the back of the motor that supports the gearbox input shaft)
  • Don't use rubber hoses for hydraulics
  • Don't activate master cylinder pistons with no fluid in them, the pistons will jam.
  • Do the wiring as early as possible.
  • Test every wire as soon as possible for continuity.
  • Don't put the scuttle on until EVERYTHING underneath it is done
  • Don't put the nose cone on until the cooling system has been tested
  • Test fluid systems for leaks as early as possible when they are easy to fix.
  • Don't leave fluids idle for long periods.
  • Get everything you can on the motor before you fit it (alternator, starter, induction, belts) - make sure it will fit though
  • Test thermostat or replace on older motors, before you fit the motor.
  • Don't fit something if you don't understand how it functions first.
  • Use the right clamps for the job (i.e specific fuel line clamps)
  • Position clamp bolts where you can reach them after the car is finished.
  • Make sure the steering rack is perfectly aligned when you fit the steering wheel.
  • Use the best fluids.
  • Always replace Nyloc nuts when you remove them.
  • If something is subject to engineering, check and understand the requirements before you start it.
  • Don't be afraid to ask or get help!
  • If something is proving difficult or not working, walk away and come back later or the next day....I guarantee you will have solved it in your head and the fix will take 5 minutes to implement!
I am sure I will add to this list as I remember other aspects of the build that have been challenging.

Thermostat

This is the thermostat  ----------------->

Its integrated with the housing. The smaller pipe on the right is the bypass. The larger pipe on the left connects to lower radiator pipe. It's currently stuck closed. This means that water circulates through the engine block and back to the bypass avoiding the radiator until the water has reached temperature. Once the water is at 89 degrees, the thermostat opens and lets water flow from the back of the engine and through the radiator, back to the thermostat. However this is not opening, so water never passes through the radiator for cooling. Best test for this is to check the bottom radiator pipe which is cold when the gauge is showing 100 degrees which is to hot.

It's a nightmare to remove (only 3 bolts) with the car completed, and it took nearly 3 hours to get it out.  I have tested it using boiling water and it failed 3 tests, then only barely worked on the last test. I will source a replacement, and test it before it goes in. Hopefully I can get it sorted and do another test run next week.

Monday, May 28, 2012

Shakedown - Part 1

I have made this post Part 1, because I reckon there is going to be a few more like it. I managed to reassemble the car after reconnecting the speedo wire so I could do the calibration. The other thing I needed to fix was the leak from bottom radiator hose. I popped the nose cone off to get to the hose clamp, and found it was not tight. I had put all the front hoses in long before I put coolant in, and never checked the tightness. Quick check of all the hoses around it and I found a similar story....oh well!


With these two problems fixed, I was able to take the car out to do the speedo calibration and just generally enjoy a drive. I organised to meet Steve and Dave, fellow clubman drivers at Steve's place which is happily about 20km away. On the  way out I did the 1km autocalibration test and found it needed 3580 pulses. With that done I had a functioning speedo.


The car went well but the trip exposed a few more problems:

  • The thermostat appears to be stuck closed....so the car ran very hot!!!
  • The muffler mount bent then broke
  • One of the headlights stopped working.
All in all a good run. We got to take some photos and it was nice to have the car out somewhere other than my front yard, especially around other Clubbies. Not major problems to fix, and I expect I will uncover more problems on subsequent runs. Best part was coming home in convoy with two other Clubbies around me!

Sunday, May 27, 2012

Troubleshooting the Speedo

I only have 3 weeks until the engineering inspection is done on the car so I need to wrap up some loose ends. One of those is the lack of speed on the speedo. I tried to calibrate it both manually and automatically on my last 2 runs but it refuses to detect a pulse. 

The speedo uses what I thought was a Hall Effect sensor, but now know is an Inductive sensor on the diff housing. The inductive pole (magnets) portion is mounted in a bracket close to the end of the CV joint bolts, and it is supposed to measure each time a bolt passes it as a pulse. You then work out how many pulses you need per kilometre and you are set.

I assumed the problem was the air gap between the sensor and the bolts, as I had not paid a lot of attention to setting the gap in my haste to finish the car (will do it later!). The gap is supposed to be between 0.3mm and 0.8mm (hard to measure I know). The problem now is to get to the sensor to reset it I needed to do a bit of dismantling once the car was up on stands. So off came:
  • Right rear wheel
  • Scuttle mount plates
  • Bottom scuttle screws
  • Interior side panels
  • Seat headrests
  • Roll cage 
  • Boot liner
Everything is interconnected hence the amount of unrelated stuff that needed to come out. I exposed the sensor, repositioned it down to a very small gap, fired up the speedo and spun the wheels to check the pulse. Nothing!

So now I pulled the sensor out and checked the resistance of the inductive component when pulsed and it is working, so now I needed to test the wiring. I reached under the scuttle and disconnected the speedo connector. With the multi meter I belled out each of the wires from the sensor to the speedo. The blue/yellow wire is showing not connected?!?!. Bugger! Remembering the rear harness connects to the body loom in the fuse box, I figured I should check the connections in there as well. So more bits came out:
  • Bonnet
  • Pod air filter
  • Fuse box lid
  • Fuse rail mount
This exposed the rear harness connector and look what I found ------>. 

The wire join for the speedo sensor had come apart and out of the connector!

Easy enough fix. Rebind the wires, add a new terminal and reinsert it into the connector. Before I rejoined each step I belled out the connection to the sensor and the speedo to make sure it was OK, and then did the same end to end connection test. Once I had the end to end connections working, I put the sensor back on and tested it again with the speedo fired up. This time I got a pulse count on the speedo! 

Then it was just a matter of positioning the sensor, final testing and then putting everything back together!

Friday, May 18, 2012

Unregistered Vehicle Permit


A UVP let's you drive the car on the road "legally" while it's still unregistered. It requires an authorized safety inspection (pink slip) and a trip to the RTA. 


The Birkin passed it's safety inspection and the nice lady at the RTA issued me with my UVP which is now proudly stuck on the windscreen. 


The only catch is it can only be driven on nominated trips for specific purposes....but at least I can now officially move it around on the road from place to place to finish off the engineering and rego process without having to use a trailer...........................................like this!


Suspension Setup


I have given Redback Motorsports a rap before, but I am going to do it again. I dropped the Birkin off on Saturday to have Greg give it a once over and also to properly setup the suspension, steering and brake balance. Over a few days he setup all of my wheel cambers, wheel toe-in, ride height, spring preload and damper rates to suit a first time Clubman driver. He also checked my brake bias setup, adjusted my steering rack and wheel position, and sorted out a few issues on the sway bars. He also rang my engineer to discuss specific tests that would be carried out on the car come engineering time, and then made sure that my car was configured accordingly. 


Greg engineers some of the quickest and best sorted race Clubmans in Australia. He has a wealth of knowledge and best of all he is a great guy to just drop in and have a chat and a cuppa with. I am lucky to have access to such a skilled engineer so close to home, and I feel privileged to have his expertise applied to my car.


The car now feels properly secure on the road, and it turns in much more predictably and consistently than it did last week. It is also riding much nicer over broken pavement and changes in surface. 


If you live in or near Sydney, and you want your Clubman sorted... properly sorted ........ take it to Greg at Redback Motorsport!




Thursday, May 10, 2012

First real drive...on the road!

Today the Birkin was booked in for it's blue slip safety inspection and a tune up. Its permitted to drive the car unregistered directly to and from the place of inspection....so drive it I did.


Unfortunately the guy who was to do the inspection was sick so I opted to bring the car home and postpone.


It worked out well as I found a few little problems on the drive.
  • Speedo is not working (Hall Effect sensor problem)
  • Leak in the lower front radiator pipe
  • Assorted rattles from the exhaust and the left headlight lense.
But it was still my first proper drive and it was fun none the less. The car feels good on the road and it really zips along in any gear. Over an hour later I am still grinning like an idiot ;)


Sunday, April 15, 2012

Finished


So after 517 days I have gone from this.........


















to this!!!!!


Let me qualify finished. Its ready to undergo testing in order to get through the engineering and registration process. Its driveable and if there was a track day tomorrow, I could now go and drive my own Clubman on the track ;)

From here the next steps are:
  • Trip to Redback Motorsport for suspension setup, wheel alignment and general checkup
  • Tune up and possible trip onto the dyno
  • New muffler 
  • IM240 emissions test with the RMS at Botany
  • Engineering check, brake test and noise test
  • VIN and Registration plates (hopefully!)

I am reliably informed these cars are never truly finished. I will still need to do the tonneau cover, harnesses (for track) and the Autometer Tach Adapter but for now I have nothing else to do in order to get it registered.

A massive thank you to a pair of fellow Birkin drivers. To Steve for all his hard work and assistance on the two person jobs, and for keeping me motivated when the build got difficult and being there for the high 5 moments. Also to Maurice who provided endless hours of advice, design photos and suggestions on specific issues via email. 

Here's a few more photos ;)